1. BigPapa TDR MEMBER

    If that one worked, the problem is in the Solas. Your truck probably doesn't have those connectors the '98.5 had.
     
    BigPapa , Oct 13, 2022
    #41
  2. Ozymandias TDR MEMBER

    FYI, you can run the engine with the valve cover off, there is no oil spray from doing so.
     
    Ozymandias , Oct 13, 2022
    #42
    Tuesdak and Dysfunctional Vet like this.
  3. Dysfunctional Vet TDR MEMBER

    Scanner is up-to-date according to my friend, he fixed his '08 with this scanner.
     
    Dysfunctional Vet , Oct 13, 2022
    #43
    Topzide likes this.
  4. MGreer TDR MEMBER

    I would try the Solas on another vehicle, maybe the scanner got corrupted along the line.
     
    MGreer , Oct 13, 2022
    #44
    Tuesdak and Dysfunctional Vet like this.
  5. Dysfunctional Vet TDR MEMBER

    I was very deliberate, and cautious when I connected the fuel injectors. I was warned (in TDR) early on in the engine rebuild project thread not to over tighten the injector connectors. That being said, earlier in this thread Topzide and Ozy both identified a good way to check the injector wires. I'll troubleshoot, I just haven't gotten back to it yet. Once I can get back to the garage I'll be checking the wires.
    I think I got a little too happy when I got my hands on the Soulus, thought that was the silver bullet...gonna fix everything antidote. Instead, it was just another scene in my epic novella.
    Just like I've gained knowledge through this forum, I'm hoping others can learn from these threads as well.

    Keep the suggestions coming, I appreciate all your inputs.
     
    Dysfunctional Vet , Oct 13, 2022
    #45
    Tuesdak likes this.
  6. Dysfunctional Vet TDR MEMBER

    Good idea, I didn't have time yesterday 'cause it got so late (and I didn't think of it), but I'll hook it up to my 07.5 and see if it connects.
     
    Dysfunctional Vet , Oct 13, 2022
    #46
  7. petersonj TDR MEMBER

    @Dysfunctional Vet , I personally would just wait until the injector block-off tool arrives. All the above-mentioned problems could be possible, but I don't think are likely because of one symptom you have mentioned - the harsh timing knock you are getting under power. To me, that strongly indicates a leaking injector for the reasons I mentioned in a previous post. In my opinion the other possible problems could cause a miss, smoke, and other symptoms, but not likely a timing knock.

    Have you pulled the oil dipstick and checked for fuel dilution in the engine oil?

    If you have a leaking injector, you do not want to run this engine any more than necessary to diagnose your problem. This is why I would not perform any other tests until I did the injector block-off test. The fuel block-off test is crude, simple, and very informative. You need to know whether or not you have a leaking injector before continuing with other tests.

    Just my 2 cents.

    - John
     
    petersonj , Oct 13, 2022
    #47
  8. Ozymandias TDR MEMBER

    One more question, and you might don't like it.
    Have you had all the openings of CP3, Rail tube and injector lines covered instantly at disassemble. And have you rinsed them thoroughly before assembly with clean Diesel or a cleaning agent and dried with pressured air to get them cleaner then clean on the inside?

    Sure that's a little late now, but after the fuel filter one needs to work like a surgeon in OP. Perfectly clean. The smallest amount of debris left in the system can and will ruin a brand new injector.
     
    Ozymandias , Oct 14, 2022
    #48
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  9. Dysfunctional Vet TDR MEMBER

    I will admit I could've kept the pump covered more, but I did try to keep it under a cover while rebuilding the engine.
     
    Dysfunctional Vet , Oct 14, 2022
    #49
    Ozymandias likes this.
  10. Dysfunctional Vet TDR MEMBER

    So I was unsuccessful in figuring it out.

    I capped each cylinder. No difference in smoke or idle on 1, 2, 3 and 6. I couldn't get the truck to start and idle on 4 and 5.

    I was successful in breaking my plastic dipstick T-handle as I leaned into the engine bay to cap each cylinder. I was also succesfull in losing a 10mm 1/4 drive socket.
    That's called Friday at my garage.
     
    Dysfunctional Vet , Oct 14, 2022
    #50
  11. Dysfunctional Vet TDR MEMBER

    Once I can stand looking at the truck I'll go back under the hood and look at wires, etc.
     
    Dysfunctional Vet , Oct 14, 2022
    #51
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  12. Dysfunctional Vet TDR MEMBER

    20221014_192548.jpg #ad
     
    Dysfunctional Vet , Oct 14, 2022
    #52
  13. Dysfunctional Vet TDR MEMBER

    Checked the injector wiring.
    They're all good.
     
    Dysfunctional Vet , Oct 14, 2022
    #53
  14. Ozymandias TDR MEMBER

    D... that gets more difficult every day.
    Checked the valve lash?
     
    Ozymandias , Oct 14, 2022
    #54
  15. Ozymandias TDR MEMBER

    How does it run when you disconnect the FCA, aka. doin a max rail pressure test?

    Some videos would maybe help to diagnose the problem. You can easily upload them to YouTube and link em.
     
    Ozymandias , Oct 14, 2022
    #55
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  16. Dysfunctional Vet TDR MEMBER

    3 times, twice while cold and once after I let it idle for 20 minutes and got it to operating temperature. All valves checked out perfect.
     
    Dysfunctional Vet , Oct 15, 2022
    #56
    Ozymandias likes this.
  17. Dysfunctional Vet TDR MEMBER

    Was I supposed to disconnect the fuel rail electrical connector when I capped off each cylinder? Because I didn't do that.
     
    Dysfunctional Vet , Oct 15, 2022
    #57
  18. Ozymandias TDR MEMBER

    No the FCA is the 3 prong connector to the CP3. If that is disconnected the pump maxes out pressure. It can be done with a decent scanner, like the cylinder selective shout down. Or by manually unplugging it.
    I'd like to know how it smokes, behaves, with more rail pressure.

    And while you are in there, please clock the CP3. It's no big deal.
     
    Ozymandias , Oct 15, 2022
    #58
    AH64ID and Dysfunctional Vet like this.
  19. Dysfunctional Vet TDR MEMBER

    So I disconnected the wire connector to the CP3 pump while the truck was idling. The truck immediately lowered RPM and started knocking badly. Smoked even more.
    Does that point toward anything?
     
    Dysfunctional Vet , Oct 16, 2022
    #59
  20. Dysfunctional Vet TDR MEMBER

    I also hooked the Solus up to my '07.5. No issues. Connected right up.
     
    Dysfunctional Vet , Oct 16, 2022
    #60
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