1. 6speed3rdgen

    i have a 03 5.9 6 speed. The truck is completely bone stock other then a fuel system and an exhaust. Recently the truck has been down on power intermittently. It has good fuel to the cp3. The injector return flow is more then below spec, about 80ml in a minute. The rail pressure relief valve is not leaking. The FCA is new so thats not the problem. I watched rail pressure on the way home the other day and it follows the target presssure pretty darn close. I seen it vary a 100 psi every now and again but nothing drastic. Another thing is the exhaust has this ticking noise. Sounds like someones in the exhaust smacking the down pipe with the firing if the engine. It seems the more down on power the louder the ticking is. Possible injector? It has gone away upon start up but is usually back within a couple miles or so. I am a diesel tech so i know my way around the truck. Im just at a loss. Injectors only have about 5-6,000 miles on them. Any help would be appreciated
     
    6speed3rdgen , Jun 1, 2019
    #1
  2. p-Bar

    Hows your boost? Throwing any codes? put a reader on anyways.
     
    p-Bar , Jun 1, 2019
    #2
  3. 6speed3rdgen

    Boost is maybe a pound lower at wide open. No codes other then lift pump circuit high cause its unplugged
     
    6speed3rdgen , Jun 2, 2019
    #3
  4. cerberusiam Staff Member

    The 80 ml per minute is an invalid number for injector return flow, redo the injector return flow test with the correct procedures as a start.

    What are your cylinder contribution readings? What is the rpm drop for each cylinder that looks off? What are the CP-3 return flow values?What ranges of load did you log demanded vs actual of rail pressure?

    Exactly WHAT were the injectors that you replaced? New Bosch? Remans? Internet junk?

    Based on your description 2 things come to mind; injector hanging open adn the charge is still firing as the exhaust valve opens, or, you have a valve dropped. Did you pull the VC, check lash and rocker position?
     
    cerberusiam , Jun 2, 2019
    #4
  5. sag2 TDR MEMBER

    Maximum return flow is 180ml in one minute. The 80ml you got should be fine.
     
    sag2 , Jun 3, 2019
    #5
  6. 6speed3rdgen

    The injector return flow spec is 180, i was just saying mine is 80ml. I havent looked at contributions yet. The DRB at work doesnt show cylinder contributions for 2003. Injectors were remans through an approved bosch dealer. Valve cover has been pulled. Nothing looks abnormal and valve lash is within spec and rockers seem to look normal.
    If it was a dropped valve wouldnt the truck run like complete garbage all the time? And wouldnt the noise be consistent? Not coming and going like mine does?
     
    6speed3rdgen , Jun 3, 2019
    #6
  7. cerberusiam Staff Member

    The typical return flow is 180 ml is 30 SECONDS at 20k psi and 1200 rpm, 80 ml in 1 minute is invalid because it is way out of the expected range.

    Return flow is not going to tell you if the injector is malfunctioning, it just indicates that the return flow circuit is not worn out. An injector that is hanging or working incorrectly will exhibit other symptoms and still have good return flow. Simply cannot base the diagnosis on just one test, you have to run thru the others to get a more complete picture. If there is a malfunctioning injector it may show on a contribution and kill test, IF the problem occurs at an idle.

    The valve seats will get loose in the head and float, really hard to diagnose that condition because it is intermittent. The knock you are describing is more than likely an injector hanging. If this is happening at an idle you should see that on contribution\kill test.

    Does not matter if you bought remans from an authorized dealer, they can and wills till be bad. I have replaced more remans from Bosch than anything else, they are just not a good choice for replacements unless you monitor constantly.
     
    cerberusiam , Jun 3, 2019
    #7
    WBraico likes this.
  8. 6speed3rdgen

    I see what you mean. Noise doesnt happen at idle. Idle is normal and smooth. The ticking only occurs through the rpm range. Usually starts at about 1100-1200 and up but goes away if you hard in it. Also does seem to occur more with boost. Only ticks with light throttle that i can hear but its hard to hear with 5 inch pipes behind your cab. If you kill cylinders 2 and 5 you can hear a major difference in idle though. Im going to see if i can borrow another techs snap on scanner and see if it does contribution test on it.

    Also if you read the test in Chrysler specs. It says idle for a minute. Should be less then a 180ml thats why i went with that spec but this wouldn't be the first time Chrysler diag has lead me wrong
     
    6speed3rdgen , Jun 3, 2019
    #8
  9. cerberusiam Staff Member

    Yeah, as a guess you have some injectors that are not working as they should in off idle operations. They should show some variations in contribution if it is a mechanical issue but not a given.

    Here is the latest injector return info I have. It is possible this has been updated but at the rate FCA is pulling all the testing protocols from their software not even sure this is good anymore. They seem to want to basically hamstring the techs form doing anything meaningful and dump all the decisions back to their resolution center for directions. They say less than 160 ml in 30 seconds is good but do not say what is expected, what I have seen is generally 160-180 ml on known good injectors. Still have to apply some logic to this stuff, this CR diagnosis stuff doesn't always follow logic closely. :)

    INJECTOR RETURN FLOW TEST @ 1200 RPM AND 1400 BAR RAIL PRESSURE
    --------------------------------------------------------------------------------
    1. Operate the engine until the coolant temperature is above 82.2°C (180°F).
    2. Turn the engine off.
    3. Remove the banjo connector from the fuel drain tube at the rear of the fuel filter housing.
    4. Install fuel system test fitting 9012 in place of the banjo connector.


    NOTE: Do not use test fitting 9014 . This fitting will block return flow from the High Pressure Delivery Pump and damage the seal and could potentially damage the engine.
    5. Install a 5/16 diameter rubber fuel hose (Hose A) onto the test fitting and into a fuel container.

    NOTE: This hose is used to measure the High Pressure Pump return flow.
    6. Remove the vehicle fuel return line (Quick connect) from the engine fuel drain tube.
    7. Install a 5/16 diameter rubber fuel hose (Hose B) onto the engine fuel drain tube and into the fuel container.

    NOTE: This hose will be used to measure the Injector return flow for this procedure.
    8. Start engine and allow to idle for 30 seconds. This step allows the flows to stabilize.
    9. Using the scan tool, navigate to ECM view -> PCM Cummins -> More Options-> System Tests -> Fuel Pressure Override Test. Select Start, then press Next.

    NOTE: While the test is running, record the FCA duty cycle % and actual rail pressure. Record the readings on the Cummins Diesel Diagnostic Worksheet located under e-files, service, Star center in Dealerconnect.
    10. Press the Run button to start the Fuel Pressure Override Test. The engine speed will elevate rapidly to 1200 RPM and the rail pressure will increase to 20000 psi (1400 bar). At this point, move (Hose B) from the bucket and insert it into a graduated cylinder.Collect the fuel until the Fuel Pressure Override Test times out (30 seconds).
    11. Measure and record the amount of fuel collected in the graduated cylinder.

    NOTE: Flow should be less than 160 ml for 30 seconds.

    NOTE: If the amount of fuel collected is greater than 240 ml/30 secs, it is recommended that all 6 injectors be replaced.
    12. If the flow is less than 160 ml/30 seconds, the test has successfully passed. If the flow is greater than 160 ml/30 seconds, but less than 240 ml/30 secs, turn off the engine and remove all 6 high pressure fuel lines. Re-torque the high-pressure connector nut for each injector. Inspect for damage, repair/replace as necessary. Reinstall the high pressure fuel lines. Re-measure the injector return flow using steps 8 through 12 as a guide. Continue on to next step.
    13. If the amount of fuel is still greater than 160 ml/30 seconds after re-torquing the high-pressure connector nuts, turn the engine off and remove the #1 high pressure fuel line. Cap the #1 fuel port using tool 9864 for the 6.7L engine on the fuel rail and re-measure the injector return flow using steps 8 through 12 as a guide. Repeat this procedure for injectors 2-6. Continue on to next step.
    14. Replace the fuel injector and High pressure connector of the injector that shows the largest amount of change when capped off.
     
    cerberusiam , Jun 3, 2019
    #9
  10. 6speed3rdgen

    UPDATE: swapped a new turbo in. Power is back and ticking is gone.
     
    6speed3rdgen , Sep 14, 2019
    #10
    WBraico likes this.
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